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Concern of Touchdown – Air India 171 Crash Triggered by Gasoline Cutoff

July 19, 2025
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On the twelfth of June 2025, a Boeing 787-8, registered in India as VT-ANB, was working as flight Air India 171 for a passenger flight from Ahmedabad to London Gatwick. The Boeing Dreamliner crashed shortly after take off, killing all the crew, 229 passengers and 19 individuals on the bottom. One passenger survived with critical accidents. An extra 67 on the bottom suffered critical accidents.

The day after, I wrote in regards to the fundamental particulars and highlighted two credible theories for what had occurred: both the plane was badly misconfigured or that each engines failed. On the time, probably the most compelling cause I may assume for each engines failing was contaminated gas, though it appeared unlikely as that ought to have affected all plane refuelling on the airport that day. I concluded that there might be an additional “one thing else” that we have been lacking as a result of the small print up to now didn’t make sense.

That sadly has confirmed to be the case and it doesn’t look good. I’m going to deal with precisely the sequence of occasions as acknowledged within the preliminary report.

Ahmedabad

The plane arrived from Delhi flown beneath completely different crew. There have been no recognized defects with the plane and the burden and stability have been inside regular working limits.

The captain held an ATPL with over 15,000 hours expertise throughout a spread of plane, with 8,600 on sort. The primary officer held a CPL with 3,400 hours of which 1,128 have been on sort. Neither had flown over the previous 24 hours.  They’d arrived at Ahmedabad the day gone by with a view to function flight Air India 171 that day. Each had ample relaxation durations. Each pilots handed their preflight Breath Analyser take a look at, which is normal process for all flight crew at Air India.

The primary officer was the Pilot Flying with the captain as Pilot Monitoring.

At 07:43 UTC (12:43 native time) the flight crew contacted ATC for pushback, which was accepted, adopted by the plane beginning up. ATC requested if the plane required the total size of the runway and the crew confirmed that they did. At 08:07:33, the plane was cleared for take-off.

The plane accelerated alongside the runway and reached V1, the take-off determination velocity, of 155 knots usually. The plane lifted off at 08:08:39 UTC. Within the air, the plane reached 180 knots indicated airspeed at 08:08:42, at which level the gas cutoff switches transitioned from the RUN place to the CUTOFF place.

The report makes use of the phrase transition, as a result of the flight information solely tells us that the place modified. Nevertheless, a vital piece of data is that there was a one second hole: one change was set to CUTOFF after which, a second later, the opposite.

This video posted to Reddit reveals the guards across the two gas minimize off switches in a Boeing Dreamliner.  What one can see within the video, which is confirmed within the report, is that to vary the change from the RUN place to CUTOFF place, you must pull every change out after which down. There are guards both facet. The purpose is that it isn’t doable to by accident knock these switches out of place.

Gasoline minimize off switchbyu/emoemokade inaviation

So, each switches moved from RUN to CUTOFF, one after the opposite. Each engines started to lose energy on account of the gas being minimize off, that’s, the report is obvious that this was a direct trigger and impact.

The phrasing of the dialog within the cockpit is necessary; right here’s what the report says:

Within the cockpit voice recording, one of many pilots is heard asking the opposite why did he cutoff. The opposite pilot responded that he didn’t achieve this.

The cockpit voice recording evaluation would come with which microphone picked up the voices: on the left or on the appropriate. Thus, it’s completely recognized which pilot spoke. The investigators made a transparent selection to not launch the precise wording or to specify which pilot requested the query.

The report confirms that the Ram Air Turbine deployed in the course of the preliminary climb, as many had noticed from the CCTV footage. This confirms that the engines misplaced energy, inflicting the RAT to deploy.

CCTV Nonetheless after take-off

The plane started dropping altitude earlier than making it previous the airport perimeter wall.

At 08:08:52, the gas cutoff change for the #1 engine transitioned from CUTOFF to RUN. The change for the #2 engine transitioned to RUN a number of seconds later. This initiates a “re-ignite and thrust restoration sequence”, that’s, the engines ought to robotically restart and start producing thrust once more.

In each instances, the engine relighting sequence began; nonetheless, it is a sluggish course of. The #1 engine was within the strategy of spooling up. The #2 engine restarted however was not in a position to spool up and recuperate thrust. Successfully, each engines responded precisely as one would anticipate to having the gas minimize off and restored. The issue was that there wasn’t sufficient time for each engines to spool again up. Had the problem occurred only a few minutes later, after the plane had gained altitude, the engines would have had sufficient time to restart and produce thrust.

One of many pilots declared an emergency at 08:09:05, calling MAYDAY MAYDAY MAYDAY.

The air site visitors controller requested for extra data however didn’t obtain a response.

The Flight Information Recorder stopped recording information six seconds after the MAYDAY name, at 08:09:11.

Accident website pbotograph from the report

The report paperwork the wreckage, principally confirming what we already knew. The Dreamliner crashed into a number of buildings and broke into items earlier than catching fireplace.  The flap deal with was discovered “firmly seated within the 5-degree flap place, in line with a traditional takeoff flap setting.”

Each gas management switches have been within the RUN place. The engine thrust levers have been discovered set to close IDLE however based on the flight information recorder, each remained set to take-off thrust till the crash, so it’s seemingly that the levers shifted in impression.

Mainly, the wreckage evaluation up to now underscores the truth that the crew tried to revive gas circulate to each engines earlier than dropping management of the quickly descending plane.

Based mostly on preliminary investigation of the wreckage, there was no fault with the plane. The report notes explicitly that there are not any beneficial actions associated to the Boeing 787-8 or the Normal Electrical engines.

The report additionally referenced Particular Airworthiness Info Bulletin NM-18-33, which has been the reason for a lot hypothesis. This 2018 bulletin was in response to numerous Boeing plane which have been delivered from the manufacturing unit with defective gas switches that might be moved too simply. This was not thought-about to require an airworthiness directive requiring obligatory inspections.

Air India didn’t examine the switches of their fleet and weren’t required to take action. Extra pertinently, nobody had reported any points with the gas switches on the accident plane after the throttle management module was changed in 2023.

The necessary level right here is that there are not any reported situations the place the switches moved themselves. It’s doable that this fault had been on the plane with out remark for 2 years. If this have been the case, it’s nonetheless clear that an individual moved these switches one after the opposite; nonetheless, it could add weight to the concept that chopping off the gas was not deliberate.

The logistics of the cockpit imply that the Pilot Monitoring was higher positioned to maneuver the switches with out it being instantly observed. The Pilot Flying, centered on the take-off, may not instantly discover the motion. The reverse, the place the Pilot Flying moved the switches, can be extra noticeable. Throughout take off, with one hand on the controls and the opposite on the throttle,  any such motion can be instantly entice consideration, particularly because the Pilot Monitoring ought to be scanning the devices and never concentrating on any single spot.

The ten seconds between the switches being moved and the query being requested appears related. Assuming that the pilot asking the query was not the pilot who moved the switches, then it appears more likely to have been a response to the engines spooling down adopted by a look in the direction of the switches to see that they have been inexplicably set to the CUT OFF place. However these at the moment are logical guesses; we don’t know who spoke, we don’t know what brought on them to talk, and we don’t have any technique to interpret the response.

Concern of Touchdown – Air India 171 Crash Triggered by Gasoline Cutoff

The preliminary report makes it clear that the investigating staff have extra proof to assessment, together with the postmortem reviews and statements from witnesses and the surviving passenger. Perhaps they are going to discover one thing that may shed extra mild on what occurred within the cockpit.

It may simply be not possible for the investigation to show who moved the switches, as they’re centrally positioned in order that each pilots have entry. What we all know: somebody moved each gas switches to the cut-off place. We don’t know who did this. We have no idea if it was a deliberate motion or a deadly mistake. Extra importantly, it will not be doable to ever know what the intent was.



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